Thanks guys. I fixed the kink -- went to a longer line as I had plenty of room. I saw the old line, and while there was a mild kink, there definitely was still enough space for fuel to pass through.
I got the engine tuned again to run, warmed up, under load, etc.
Seems the culprit is the adjustable main jet that I installed. People were right - seems I'm going to be constantly adjusting this thing! Argh.
I wonder if I should just go back to a fixed main jet. Theoretically, I should be able to set the adj. main to the exact same specs as the fixed jet right?
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1975 Bristol 30 Sonora del Viento
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